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  Home > Resources
Source Newsletter spring 2001  
 

Brewing Up Prevention ideas

The St. Paul brewery has saved nearly $400,000 a year over the past four years by working on pollution prevention with SERVICE Environmental & Engineering.

MBC which produces various brands of beer and water reopened its 136 year old facility in 1991. The brewery wanted waste reduction alternatives with minimal to no capital investment. It considered options, progressively, with capital paybacks of less than three months.

The consulting firm teamed with plant production and engineering personnel to identify all major water and chemical flows within the plant. A plant-wide assessment identified all leaking valves and uncapped pipes. Every major flow was evaluated. Non-contact cooling water discharges were considered for reuse in other parts of the plant. SERVICE identified three potential areas for significant savings.

Water Use
The Minnesota Brewing facility was designed for a three-shift continuous production schedule. Initial production volumes were lower, but the water flow control and metering systems were not configured for the lower volumes.
Adjusting production steam and water flow to match current production needs saved MBC $200,000 a year in water, sewer and energy costs.
Numerous leaking valves and open pipe discharges of non-contact cooling water were identified. Low cost repairs saved 158 gallons per minute with annual savings of $82,000.
A meter that was out of calibration over-recorded water use. Replacing the meter saved $50,000 a year in excess sewer charges.

Chemical Use
Because water flow was not calibrated to current production levels, excess amounts of chemical were used. Some feed pumps discharged excess chemical because they were out of adjustment or not synchronized with operations.

Chemical suppliers quickly volunteered their assistance, adjusting the chemical feed mechanisms to match the current flows and to shut off when not in use. This reduced chemical costs by 50 percent, or about $15,000 per year.

Product Loss
Product loss was higher than industry standards because the brewery's distribution pipes were designed for greater capacity than current production. To reduce product loss, equipment manufacturers and SERVICE adjusted the filling equipment and developed filling protocols. Cleaning methods were devised so pipes could be purged of product before being washed with cleaning solutions. Minnesota Brewing has reduced product losses, saving $6,000 a quarter. To reduce sewered waste, MBC is evaluating having wasted product recycled into ethanol.

 

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