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  Home > Resources
Source newsletter spring 2003  
 

Site Visit—Cooling Down with Water

With summer on the way it won’t be long before we are cooling off on a hot day by jumping into a lake or taking a dip in a swimming pool. As more people use the pool to beat the heat, using water to keep people cool becomes more economical.

Water is also a great way to keep things cool in your operation. And just like the swimming pool, the more times the same water is used and reused to keep things cool, the more economical it will be.

Cooling water increases
Alpha Ceramics, Minneapolis, produces specialized ceramics for sonar and medical diagnostic ultrasound applications.

To make the product, ceramic materials are mixed then cycled through high temperature and pressure in a kiln. Water is used to keep critical parts of the kiln cool during its high-temperature operation. Cooling the company’s six kilns separately used about nine million gallons of water per year, making it one of the facility’s main uses of water.

Alpha Ceramics was facing a SAC fee of $8,000 because of increased water use. The facility’s other water costs included water purchase and sewer fees of over $5,400 per month.

The company planned to install six more kilns to help meet production demand. But, it needed to cut water use before installing more kilns.

MnTAP engineers, Randy Cook and Karl DeWahl visited Alpha Ceramics to help. “They gave us some good suggestions about where to reduce water use. Their ideas helped expand our thinking and gave us a new perspective,” said owner Jim Sloane.

Same results, less water
The company tested reuse of the cooling water. Cooling water passed from the first kiln to the second then a third before becoming too warm.

After seeing the results, the remaining three kilns were plumbed together in a series. Reusing cooling water will reduce water use to one-third of its original demand.

Cost and savings
The changes were handled inhouse at marginal expense in labor and materials. Once in place, the plant reduced wastewater from 29,000 to 11,000 gpd. This helped avoid the SAC fee. Yearly water use at Alpha Ceramics was reduced by 6.57 million gallons. The company saves $40,200 annually in water use and sewer fees.

“We have probably gone below our permit restriction and when the new six machines are added it won’t increase our water use [beyond the permit],” said Sloane.

Get customized suggestions for your operation.
Request a site visit from a MnTAP engineer or scientist. Call 612.624.1300 or 800.247.0015 from greater Minnesota.

 

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