Gold University of Minnesota M. Skip to main content.University of Minnesota.
 
Minnesota Technical Assistance Program
Intern Program
Materials Exchange
Resources
Wastes
Industries
 

Dry Cleaning

Energy Conservation

Fiber Reinforced Plastics

Food Processing

Health Care

Iron Mining

Laboratories

Machining & Metal Fabrication

Metal Finishing

Metalcasting

Painting & Wood
Finishing


Paper Mills

POTWs

Printing

Vehicle Maintenance

Water Conservation

 

 

 

MnTAP logo   612.624.1300
  800.247.0015
 
  Home > Resources
Source newsletter spring 2003  
 

Interceding for St. Jude

St. Jude Medical’s Maplewood facility manufactures heart valve components. An important step in its manufacturing process is pyrolytic carbon coating of the components. In this process, cooling capabilities are critical to ensure product quality. Through 2001, coating reactor cooling was accomplished with an average use of 20,000 gpd of city water. Most of this water was then used to clean screens in the associated scrubber. Changes in city water temperature and pressure required operators at St. Jude to monitor reactor temperatures closely and adjust water flows frequently.

Karl DeWahl, MnTAP engineer, visited the St. Jude facility to help maximize efficiency. “Karl was very detailed. He recommended changes to help us reduce water use and save money,” said Mike Jackson, coating engineer at the Maplewood facility.

Gaining control
The big change Jackson wanted was implementing a recirculating cooling-loop system he designed to gain better control of the coating process. This system consisted of three 5,000-gallon storage tanks with pumps, piping and temperature controls to circulate the water through the reactors and back to the tanks. The volume of water in the tanks is sufficient to cool one day’s production with no outside cooling needed. It also provides a backup supply so that repairs could be made without shutting down the coating process.

Installed, the new cooling system cost $120,000 and reuses about 10,000 gpd of water from the coating reactor cooling for makeup to the scrubber.

Avoiding a SAC
When Jackson recommended his recirculating cooling-loop system, St. Jude was faced with a one-time SAC fee of $85,000 for increased water use. Avoiding the SAC fee was a big incentive for the facility to implement Jackson’s design. The facility also saves $20,000 annually on water use. The new system design had a projected payback of two years.

According to Jackson, “Five million gallons of water per year in the coating process has been reduced. [This is an] 80 percent reduction in the department’s water demand and about a 50 percent reduction for the entire facility.”

“Implementing this system reduced long term operating costs and gave us a stable and reliable cooling water system and also resulted in improved production yields,” concluded Jackson.

 

MnTAP logo

 

MnTAP Publications
- Source Newsletter
- Permission to Reproduce
P2 Planning
————————————
Business Awards
Calendar
Financial Assistance
Links
Regulatory Resources



 
 
The University of Minnesota is an equal opportunity educator and employer.