Gold University of Minnesota M. Skip to main content.University of Minnesota.
 
Minnesota Technical Assistance Program
Intern Program
Materials Exchange
Resources
Wastes
Industries
 

Dry Cleaning

Energy Conservation

Fiber Reinforced Plastics

Food Processing

Health Care

Iron Mining

Laboratories

Machining & Metal Fabrication

Metal Finishing

Metalcasting

Painting & Wood
Finishing


Paper Mills

POTWs

Printing

Vehicle Maintenance

Water Conservation

 

 

 

MnTAP logo   612.624.1300
  800.247.0015
 
  Home > Resources
Source Newsletter 2004 issue 2  
 

Filtering Out Waste

Paint was “hanging” in the booth, causing Crenlo’s painters to complain about overspray and poor airflow.

“If anyone complained about booth conditions, we changed out the filters rather than knowing what our problem was, “ explained Jason Kleeberger, safety/environmental specialist. “We had no set procedures.”

Crenlo LLC fabricates sheet metal products, including agricultural and construction equipment cabs and electronic enclosures.

Test panels located on the top of the exhaust stacks showed paint, possibly indicating low paint-capturing efficiency for the filters. The back layer of the filters were discolored by paint making it look as if the filters were loaded with overspray.

All of these factors led Crenlo to change its paint filters daily. At roughly $1,000 a day, the filters were exceeding the amount budgeted. Excessive maintenance time was also required for filter change out. Crenlo requested a MnTAP intern to help investigate and reduce its paint filter waste and to decrease its wastewater volume.

The intern analyzed the system for best set up. He tested different types of paint arrestors. None of them performed better than the two different layered grades of high efficiency/high capacity paper filters that Crenlo was currently using.

The intern also experimented with the frequency of filter change out. Depending on the paint line, he was able to extend the use of the top filters to three or five days without measurable change in efficiency. The bottom filters could last 12 days.

Based on production levels at the time of the intern project, modifying the paint filter change out schedule saved Crenlo $95,600 a year. Filter purchase cost was reduced by $88,200 and waste disposal was reduced by 21 tons a year, saving $7,400. Over 1,500 hours of maintenance labor was no longer needed to change out filters. Crenlo also made booth repairs to prevent air leaks.

The challenge for the intern was dealing with busy maintenance supervisors. “If Yafet [the intern] came to talk to you, he’d ask one or two questions. Yafet was able to get the information he needed—fast,” said Kleeberger. “He could work on his own. You didn’t have to hold his hand.”

More information on paint filters is available in Paint Filters: Crenlo saves Nearly $100,000 by Reducing Paint Filter Waste and Water. Intern program application deadline for 2005 is March 1; see the MnTAP Intern Program Web page.

 

 

 

Other Source Issues

 
 
The University of Minnesota is an equal opportunity educator and employer.